Derek's front 8" clam gets cryo treated 488 Nitro thick gears and an upgraded collar. |
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(67 BIG pics loading) |
DEC 24 2017 |
This arrived from JustDifferentials.com |
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Everything needed to regear the front and rear diffs in the FJC to 488. The gear package from JT's basically consists of 4 boxes and 2 solid collars in baggies. This kit works great as long as the original gears are the 373 ratio. If the oem gears are 390 or 410 then a new carrier with the lower deck height would be needed....something ZUK probably has. |
The above picture shows the carrier split that only the 8" clamshell has. The oem 373 carrier on the right has a lower deck height.... the 11 tooth pinion is much larger in diameter so the ring gear has to move farther away and that carrier allows it to happen. |
The rear 8" on the left....front hi-pinion reverse cut ring/pinion on the right. They will be at Cryogenics International tomorrow. |
Derek sent his diffs to me here. |
Gears are back from cryo. Derek's front clam....488 gears....Nitro master kit....and the solid collar. |
Remove the un-needed stuff. |
This short axle stub comes out easy.... |
...from the other side. |
Easy as butter. |
Take the 10 bolts off that secure the lid. |
Lid's off. |
Remove the 10 flange style ring gear bolts. Good luck. Better have a really good socket and a really super impact wrench. |
The thick Nitro 488 ring is now installed. Careful alignment initially to get the bolt holes to be in perfect alignment. |
Lots of tapping with the lead filled plastic hammer to seat the tight ring gear. |
85 ft/lb per the FSM with blue loctite. |
New Koyo carrier bearings were really a tight fit but this hammer was up to the task. This end done. |
Now onto the pinion end. Remove the flange. |
Press the old 373 pinion out. |
There is a special tool to pull the inner pinion race in place. As far as I can tell, it's not needed. < I have no trouble using a stub hammer that fits in the limited space. |
Fully 100% seated down and no damage. |
The outer race is even easier. |
Starting with a .0775" pinion shim on the new bearing. |
Lots of gear oil on the pinion bearings and tighten the pinion nut only enough to get about 15 in/lb bearing preload. |
A quick way to determine if the backlash is even there....place the center carrier in and check for wiggle. There was none here so can't run a paint test without backlash. |
Using that just perfect scrap bearing part.... |
....Tap out the washer plate from the "bowl" and in my case here, went from a thin .069" to a .083". And change out the washer plate on the lid side also. Without a good washer plate selection, this can become a frustrating task. Fortunately, I have a near full selection :) |
Bolt it all back together. |
So, with the lid bolted down....at least some carrier bearing preload....at least some backlash values in the ball park.... |
I got lucky...only had to change the washer plate on each side only once to get a preload of about 5 in/lb and have a snug backlash of .005". This is good enough for a paint test. |
I already had painted 3 teeth ahead of time, and now, to offer resistance on the pinion flange while turning the sidegear with a cheater bar. |
This gives me enough contact resistance to get an easy to read paint. Here's the drive side and it's a bit too deep.....centered but deep. |
The coast appears too deep also. |
Drive....reverse painted. |
Coast....reverse painted. |
The comet tail on the pinion tooth is way too close to the face of the tooth(edge). |
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Let's try something thinner like .073" |
Good time to increase the thickness of the washer plate in the bowl by .002" (from 083 to 085). That will open up the backlash a little more....as well as increase the preload a little more. |
Repaint the teeth... |
Repeat and turn the cheater bar back and forth 3 times. Remove the carrier and this is the result. This is with a pinion depth shim of 073. Just a touch deeper than I want so will use 072 and that will be the winner. |
Coast |
Drive....reverse painted. |
Coast...reverse painted. |
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More backlash checks....all looks in spect at this point which is almost the endpoint. |
Now to finish up the pinion end, we just need to put the solid collar and seal in. |
Took about 5 times to get the shimming right on the collar....typical. |
With the shimming set it's just a matter of supporting the pinion in the hole... |
...and tap the outer bearing in place and put the seal in also. This is a good seal...THO....Made in Japan. So we will use it. |
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The THO seal is next. |
Recessed down .190"....evenly. |
The oem flange was in excellent shape but #1500 sandpaper still made an appearance. |
The high accuracy torque meter measured a smooth 10 in/lb. |
FIPG for the lid. |
45 ft/lb per the fsm with blue loctite. |
The new drivers side seal is tapped in. |
Looks good. |
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Notes. |