Local NC Landcruiser install goes bad fast...."ZUK, can you dissect the install and give it a proper set up?" |
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(87 BIG pics loading) |
AUGUST 20 2018 |
Nick, out of North Carolina, had "a friend of a friend of a friend" do his front FJ80 install. Only 20 miles of easy break-in and the 3rd starts making a loud noise. A few emails and 5 days later, I receive the box. |
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A nice job of cushioning the 3rd in all planes. |
Initial inspection shows too much thread exposed. This basic style of nut requires a thick hardened washer and that was missing. |
Some damage to the bottom of the nut and the once new triple drilled flange. |
There were no paint marks from the original install so not sure how anybody can even call that a gear install but I did paint the teeth here and this drive side shows wayyyyyyyyyy deep. The pinion shim is much too thick and not casually so. |
Coast side....terribly deep also. |
Backlash was actually in spec though. Nothing too special to say about the bearing preloads....they were not wobbly and seemed normal. |
Pinion tooth has the contact on the extreme tip/edges. |
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Guess I won't be re-using that nut again. |
The flange's sealing surface looks almost perfect. |
No hardened washer and this is the result. In this case, it's mostly cosmetic damage. |
This was a new 27 spline Yukon seal. |
This bearing and the race look older than the 60 miles put on them and that could be the result of excessive metal debri in the new oil. |
A crush sleeve was used. |
The shim value used was .079" which is a very typical shim. |
A closer look at the small outer pinion bearing/race. |
The large inner race has damage consistent with metal particles in the oil (contamination damage). |
Damage comparisons of the inner and outer pinion bearings. |
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The carrier bearings are turning about 5 times slower but have similar damage to the race and bearing rollers. |
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Out with the old and in with the new.....time for new Koyo bearings from the Nitro kit. |
There was damage to the pinion threads but I had the fix. |
The new nut would now spin on effortlessly. |
New inner koyo race tapped in with 360 degree support. |
Same with the smaller outer race. |
Going to try a much thinner .061" pinion shim now. |
The pinion assembly station...... |
Just tight enough to develope about 20 inch/pounds of pinion start torque. |
The design of the journals and surrounding area is such that a puller cannot reach in there and get the bearing off. |
A dremel with a grinding wheel can do it in 5 minutes. |
Bingo! |
Easy peasy. |
To the garbage can. |
The fine metal mush that the electro-magnet attracted to it in the previous weeks is visible on the inside edge of the grey ring. I will have to dis-assemble the magnetic body and clean it. |
The cage is removed... |
The inner race is also removed. |
A screwdriver and that "just right" roll pin punch allows the pressed on ring to slowly be worked up. |
A slightly larger roll pin punch allows the sleeve to work up farther.... |
....until it is free and clear. |
That's not my mess....that's what the electro-magnet attracted to it while the ring/pinion were meshing terribly together. |
2 small screwdrivers and the coiled clip can be worked loose. Kind of like taking a tire bead off a wheel. |
It's free. |
Yucko....this is why I had to take it apart and clean it. |
Everything is totally undamaged and the particles will be blasted off thoroughly with my favorite sauce.....pressurized starting fluid. |
This needle bearing might be considered the wear item with all that debri in there....but it will be squeaky clean when I get done. |
This "ramp ring" gets cleaned also. |
cleaned and oiled up. |
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Coiled spring is easy to reseat it.....start here and work 2 screwdrivers around. |
Lastly, the sleeve retainer. |
I found that just right bearing "widget" and lightly tapped the sleeve down til it was seated 100%. |
100% down. |
Now the new Koyo TR100802-2 bearing is tapped on. A nice, tight fit at that. |
This section is now complete. Now to load this Harrop into the 3rd and paint a few teeth. |
Drive side 061..........Even with a much thinner .061" pinion shim the contact is still too deep. |
Coast 061....way deep still. |
Now to really, really go thin.....25 and 11 makes 36 so let's try .036" shim. |
Drive side 036.....We just overshot it by a little....now shallow. |
Coast 036....shallow. |
Now trying .049" |
Drive side 049....deep now. |
Coast 049....too deep. |
Zero'ing in on it....Driveside with .042" and this is perfect. |
Coast with 042 and it's very nice. A keeper. |
Drive side reverse painted. |
Coast reverse painted. |
Drive side of pinion tooth....comet tail is feathering towards the center(from the root) so it's perfect. |
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Solid collar time. |
Most of the time the oil retainer hits the edges of the solid collar. |
Leaving out the oil retainer is one way to avoid contact but one could also flare the retainer up a little with this tool. Looking closely, you can see that the retainer has been flared up by using this tool on the bottomside. |
That, in combination with some relief on these abrupt edges, allows for plenty of clearance. |
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I got lucky, it only took 2 tries to get the collar shimmed correctly. |
The collar is also clearancing the oil retainer just fine as shown. |
Fan-blade slinger and Marlin Crawler seal time. |
The Marlin seal is the seal of choice for the 27 spline rear Landcruiser 3rds. Oil is applied to the rubber and flange goes on. |
Even with all the lubricating anti-seized used, it still took about 190 ft/lb on the nut to get the desired 10 inch/pounds of pinion bearing start torque. |
Bearing caps are torqued to 70 ft/lb, wheel adjuster are set for carrier bearing preload, and backlash is then recorded on every other tooth. |
Some specs are inscribed. |
Lastly, the tabs are torqued to 10 ft/lb |
The wiring was a little short so I offered to extend them about 6 inches. I have 2 solder certs from Hughes Aircraft Company Tucson AZ so I put that skill to use ;) mil-std-2000 |