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Mike is local to me so he tore into his truck, removed the rear diff, and showed up at my shop....
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....the plan is to use a 529 Yukon and an Aussie Locker, all new bearings, and a solid collar.
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Step one is to remove the bearing caps...
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I'll work on the case last and get the pinion end ready to go.
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Even though the nut was well-staked, the electric impact took it off in about 1 second.
This tool has paid for itself many times over.
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I have a soft chisel and this does not damage the race while it's being tapped in.
edit---Best to stay away from all punches/chisels...
use an old race to evenly "pat down" the new race.
Using a punch could result in "oscillating" pinion
preload measurements with the torque wrench.
1-8-2011 ZUK
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The larger inner race is is a little trickier to get it tapped in straight but doable.
edit---Best to stay away from all punches/chisels...
use an old race to evenly "pat down" the new race.
Using a punch could result in "oscillating" pinion
preload measurements with the torque wrench.
1-8-2011 ZUK
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I'm skipping a few steps here but I loaded up the pinion with a .082" pinion depth shim. I pressed
the inner pinion bearing on then slipped the solid collar on with .066" worth of shims. I then
mounted the pinion in the case only to find out that it was loose on pinion pre-load so, in the pic
above, I am now pressing the pinion out to reduce the shims on the collar and try again.
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On the 3rd try, using .058" for the collar shim, I was right at the
desired 10 in/lb of pinion drag.
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Back to the case...with the bearing puller in place, I quickly realized that the bearings required
very little coaxing to get them off. They just about fell off. I will use the Loctite Sleeve
Retainer compound with the new bearings.
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Bearings are off...ring gear is off...Time to install the Aussie so I have removed
the center pin here.
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The spider gears in my hand are no longer needed...
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The factory sidegears also are not used. The thrust washers both measured .067" thick
and they do get re-used. Some people unknowingly leave them out and then the locker does
not operate properly.
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The first step is to check a tolerance listed in the Aussie assembly manual.
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Using feeler gauges, all 4 spots are checked and found in spec. I was able to slip a
.014" feeler in there and the spec wants to see between .006" and .016".
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The couplers would not go in...
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I used a large rat-tail file to remove some material...
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...and then it slipped right in.
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Line the drive couplers up and insert the 4 pins.
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With the pins in place, now it's just a matter of installing the springs.
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I find it easiest to line this end up first...
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...then tap the other end in with a small screw-driver.
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I checked the second tolerance and all was good.
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Slip the power pin in place and tap the roll pin and the Aussie is done.
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I applied Red Loctite on the new ring gear bolts and 75 ft/lbs of torque.
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I used starting fluid to clean the surfaces and applied the sleeve retainer compound. For loose
fit bearings, this will "lock" them in place and prevent spun bearings.
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With the case in place, I ran a pattern...drive side...looks a little on the deep side.
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coast
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I tore the diff down and removed .002" off the pinion depth shim...this is much better.
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coast.
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While I turn the pinion, I rap on both bearing caps numerous times to shake the carrier bearings
into an equal tension state. This helps with accurate backlash measurements.
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Markings on the ring gear to help identify these particular ring and pinions...
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My notes during the install...
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Done :)
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